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Cost Saving areas in Textile Spinning, weaving ,Dyeing and boiler using industry. Electricity Saving Maintenance cost Thermal energy Water saving Miscelleneous Electricity Saving in Mill air conditioning Humidification Mixing the return air By removing the air load In O-End chiller Lab humidifier by misting can after the supply fan can caused by dust fans about 50- 80 kw eliminate the need save energy for from a 100 kw filter in out of a 100 Kw 1.5 to 2 kw for pumps and inv the supply fan. the Blow room, we Chiller can be can be repalced erters across all can save approximately saved/day by 100 wats departments, resul 30 kW of energy." or less ting in significant *A new concept *A new concept *A new concept device. energy savings of approximately 50 kW. Maintenance Thermal energy Water saving cost Saving saving. We can eliminate show Yarn conditioning cold The cost of heating makeup ...

Cotton spinning-cost saving, Autocone, misting use in humidification plant.

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 Misting system for humidification reduces maintenance, electricity, and water consumption costs. The system is simple and needs only a few misting nozzles, and line water to make a mist using compressed air or a high-pressure pump of about 200 bar to push water through a small orifice nozzle at about 40 to 50 bar. The Nozle choking can be avoided any using a special design of nozzle used by compressed air and produces about 10 to 20 microns of mist. In the Auto cone, of cotton spinning mill uses misting to maintain about RH% 65 and around 96 degrees temperature without using the below-mentioned parts which need maintenance and consume near about 100 units of electricity/day in the dry season. Humidification, without using a 7.5 Pump, Inverter, M.s header which needs to be changed after running few years in water, about 24 PVC Pipes, 150 showering Nozles, Clamps, and Nozle plates, and no need to drain about 2000 L water every month.No chemical treatment expenses are needed for tank...

Cheap solutions in cotton spinning mill

Blow room: 1- Most of the mills have a fire or spark-catching system installed, and its water level and cotton level sensors got damaged. Each of them normally costs 300 USD. It can be replaced by just 1000 to 2000 Rupees only i.e. in about four to six $ 2- Some wire beaters have a small motor to control cotton waste by moving the trash knife or wing, If the wing moving motor gets damaged and does have not in spare then hold and fix the knife by a bolt, adjust the gauge manually, and run the machine. 3- If a Chinese plucker's beater up-down motor is damaging brackets or wheal bracket too much then check if the up-down motor is moving when the plucker is stopped when feed is not required by the subsequent machine, maybe it has stopped over the sensor which gives pulse to go down after every turn if it is the case then the beater up-down motor will start going down and down because the sensor is continuously on so there should be interlocking in such a way that when the plucker is st...

Cost saving in humidification

  Exploring Humidification Technologies for Effective Cooling and Desired Humidity Levels Introduction Maintaining proper humidity levels in various environments is crucial for both human comfort and the preservation of materials. In regions with low humidity, achieving optimal humidity levels can be challenging. This is where humidification technologies come into play. Among these technologies, mist and fog showering have gained popularity due to their cooling effects and ability to achieve desired relative humidity (RH%) levels. In this blog, we'll delve into different humidification technologies and their applications, focusing on the benefits and drawbacks of each approach. Types of Humidification Technologies 1. Immersed Electrode Humidifiers These compact devices are commonly found in environments where precise control over humidity levels is necessary. Immersed electrode humidifiers work by heating water to produce steam. The quantity of steam generated is proportional to th...

ٹیکسٹائل میں بچت کی اقسام:

لاگت کی بچت کی اقسام: الیکٹرک پاور، روایتی مکینیکل حصوں کو ہٹانا۔ 1- نمی والے پلانٹس میں برقی توانائی کی بچت (500 یونٹ فی دن)۔ 2- بلو روم کارڈنگ روٹری فلٹرز میں برقی توانائی کی بچت۔ 3- ٹیکسٹائل پروسیسنگ میں پانی کی حرارتی لاگت کی بچت۔ 4- HHO انجیکشن لگا کر بجلی کی پیداوار میں گیس، ڈیزل اور پیٹرول کی بچت۔ 5- اسکریپ کو پگھلا کر شافٹ وغیرہ بنانے کے لیے 2000 ڈگری سی فرنس بنانا۔ نمی میں: درج ذیل ٹیکنالوجیز کا استعمال بجلی کی کھپت اور دیکھ بھال کی لاگت کو کم کر سکتا ہے۔ a- مسٹنگ نوزلز کے ذریعے پانی کو ایٹمائز کرنا، ایٹمائزیشن تکنیک تقریباً 1000 پی ایس آئی کا ہائی پریشر پمپ اور تقریباً 0.1 ملی میٹر مسٹنگ نوزل ​​ہے۔ اس سسٹم میں نوزلز کا دم گھٹنے کا مسئلہ آتا ہے۔ لیکن بخارات کی ٹھنڈک میں استعمال ہونے والے پمپ کی طاقت کا نصف کم کر سکتا ہے۔ b- کمپریسڈ ہوا کے ذریعے واٹر ایٹمائزیشن، یہ سسٹم باریک مسٹنگ نوزلز کا بھی استعمال کرتا ہے لیکن کوئی پمپ، انورٹر، ایم ایس ہیڈر، 24 شاورنگ پائپ، اور تقریباً 150 سے 300 شاورنگ نوزلز کا استعمال نہیں کرتا۔ لہذا برقی توانائی کی بچت کے علاوہ یہ پمپ، ہیڈرز ن...

saving tip Spinning-Textile, 500 units of Electricity/day and about 15000 L of water,

  Introduction: The research and development (R&D) team has successfully completed several tasks aimed at continuous improvement and cost-saving measures. By utilizing the Total Quality Management (TQM) system and fostering a proactive mindset among the employees, achieved significant results in terms of cost savings and energy conservation. This progress report highlights the completed tasks and outlines future R&D initiatives. Completed R&D Tasks: Formation of TQM Team: A dedicated team was built to focus on continuous improvement and cost-saving initiatives. This team consists of enthusiastic individuals from various departments within the organization. Cost Savings: Through various R&D efforts, achieved cost savings of above Rs 5 million. These savings were accomplished by finding inexpensive alternatives to expensive and unavailable parts. Electricity Savings Target: The R&D team's goal was to save about 500 units of electricity daily. successfully ide...

Benefits of R&D Team in an organisation.

  Benefits of R&D Team in a Spinning Mill: Continuous Improvement: The R&D team's primary focus is on continuous improvement, which fosters a culture of innovation and efficiency throughout the organization. By constantly seeking better alternatives and solutions, the team drives the company's progress and competitiveness. Cost Savings: One of the significant benefits of having an R&D team is the ability to identify cost-saving opportunities. By exploring alternative materials, processes, and equipment, the team can significantly reduce expenses, as seen in the above-mentioned achievements of above Rs 5 million in cost savings. Energy Conservation: The R&D team plays a crucial role in identifying energy-efficient practices and technologies. By setting targets such as saving 500 units of electricity daily, the team helps the spinning mill reduce its energy consumption, leading to lower operational costs and a reduced environmental impact. Technological Advancemen...